router

Mat drilling contraption report

Another attempt to kill several birds with one stone:  

  • Test belt-driven mini-router design
  • Test solutions for motor coupling backlash (Oldham coupling, pulley on motor shaft)
  • Drill the cutting mat in a few hours

The mat drilling contraption is basically the new belt-driven design of the mini-router, with the exception of Z-axis which is also belt-driven (mini-router still uses leadscrew on Z-axis). Dremel flex shaft with the drill chuck and 1/32" bit is mounted to Z axis. The results are rather mixed. 


Mini-router tests - drilling vacuum table for paper prototyper

After milling tests, I tried drilling out small hole pattern in the cutting mat (which would make a vacuum table surface for the paper prototyper). Initially I used tiny 0.01" drill bit and drilled a short sequence of holes, only to realize that there would have to be 50x50 grid of 0.01" holes spaced at 0.01", i.e. 2500 holes per square inch. Even without doing the math it was clear that it was going to take forever to drill out 8.5"x11" rectangle on the mini-router, so I switched to 1/32" drill bit, with more realistic 16x16=256 holes per square inch. This would take forever/10 in theory. In reality, one square inch took 10 minutes to drill at 12 IPM which wasn't that bad. Still, at 6 sq.in/hr it was going to take about 20 hours to drill the letter paper size area + 1/2" outside margin.

Mini-router tests - milling soft wood, delrin with Dremel

Here come more mini-router tests - mostly milling soft wood, trying some Delrin. I've run into several issues along the way - they slow down the progress some, but on the other hand they are good learning experiences. 

Dremel runout 

First, the grooves that I initially milled with high speed cutters were about 0.02" wider than the tools. I googled "dremel runout" and found various bits of information, ranging from "Dremel is no good because of runout", to "Runout is much better with chuck as opposed to collet".


Mini router endurance test (fail)

After replacing Home Depot leadscrews and finishing the assembly of the mini router, I ran an initial endurance test. The test consisted of drawing 1/4" grid on 8"x10.5" rectangle, rapid repositioning, then drawing 64 concentric circles with 1/16" spacing in the middle of the rectangle. The feedrate was set to 17 IPM (~7mm/s) while rapid movement was set to 20 IPM - not really rapid, but it was the fastest considering that motors stalled at 25 IPM. At 17 IPM the test was going to take some 1 hr 30 min or so. It ran for an hour - the Y axis stalled about halfway through the concentric circles. The rapid repositioning also didn't work too well since the circles were shifted relative to the grid in both X and Y - I have not yet figured out by how much exactly.

The video is 16x realtime. Y axis stall happens in the very end at 4:20.


Mini-router assembly progress

This is mini-router assembly in progress. The Y, Z and X stage are already assembled, working on the base now. I wanted to do a video timelapse of the whole thing, but as I went into several dead ends where I had to go back a couple of steps and re-assemble or re-align something differently, I thought I'll do clean timelapse when there are documented steps.

I've also had several issues with the assembly that aren't showstoppers but are still important:


Milling HDPE

Milling plywood was relatively easy. Plastic - a bit more difficult. First, I tried cutting shapes out of black 1/8" thick sheet of what turned out to be polyethylene, according to this plastic id table. I used the same high speed cutter as for plywood - Dremel #194, speed setting 4 and 0.03" depth passes at about 9 IPM. There was a lot of plastic swarf. Then I tried milling a 3/8" thick cutting board made from HDPE. The stuff started melting and forming blobs around the bit, even though I used recommended speed setting (4). After  experiments with speed and feedrate, and online research (good plastic milling info), I switched bits. I wanted to cut gears for RepRap extruder out of HDPE, so I got some small diameter bits on eBay to try.

First minirouter tests

Finally, here goes: minirouter and first tests with Dremel on plywood. The router had actually been assembled for weeks - it only took me several evenings to assemble it, but few problems came up and I spent time trying to fix them, then fixes/workarounds resulted in new problems and so on. The same flaws and weak spots mentioned in the previous post still remain in the design. Couplings is one of them, and non-alignable leadnut is the other.

 


Next steps

I haven't posted in a while, but have done a few things:

Taken apart the drilling contraption since I didn't really need it when the angle no longer had to be accurate; enlarged to 1/4" the holes on the angle from drilling contraption. This created a nice pile of Contraptor parts, ready for the next project. Made several sliding elements of different sizes - full, half, "quarter", installed Delrin nuts in some of them. Revisited the whipping rod/nylon couplings problem and decided to switch over to 0.250"ID aluminum tube for couplings. Tried to couple this tube to 10-24 rod, unsuccessfully. Searched for more powerful but still cheap steppers with lower coil current. Plotted the next contraption to be built.