
I haven't posted in a while, but have done a few things:
Taken
apart the drilling contraption since I didn't really need it when the
angle no longer had to be accurate; enlarged to 1/4" the holes on the angle from
drilling contraption. This created a nice pile of Contraptor
parts, ready for the next project. Made several sliding elements of
different sizes - full, half, "quarter", installed Delrin nuts in some
of them. Revisited the whipping rod/nylon couplings problem and decided
to switch over to 0.250"ID aluminum tube for couplings. Tried to couple
this tube to 10-24 rod, unsuccessfully. Searched for more powerful but
still cheap steppers with lower coil current. Plotted the next
contraption to be built.
Quarter inch holes in the angle are
working out pretty well. When assembling something, distances and right
angles may need adjustments with tape measure and a try square, but
it's better than trying to put a screw through 2 holes of just the
right size that slightly don't match up. Oversize holes make
manufacturability at home much easier, which is an important goal of
the project.
New couplings

When I switched to nylon spacer
couplings between 1/4" rod and 10-24 rod, there was still some wobble
in rotation. Eventually I tracked down this problem to 2 things: first,
when you thread small nylon spacer onto the 10-24 rod, it's never
perfectly parallel. This becomes visible when rolling the small spacer
with 10-24 rod on a flat surface. Second, the inner diameter of the
large nylon spacer is slightly more than 0.250" - which means that the
ACME screw and the motor shaft can move in the radial direction inside
the spacer. Also, the thread in nylon could be easily stripped, so I
could not really tighten the set screws. I was working around these
problems by wrapping some electrical tape around the motor shaft or
ACME screw, and drilling deep set screw hole, going into the rod
itself. That kinda worked but only when the coupling was first made.
Because the set screw holes were not at the exact right angle to the
coupling axis, large spacers slanted if they were not drilled together
with the rod. I had thought about making a coupling from aluminum (so
that deep set screw holes would not be needed), but could not find
appropriately sized tube on McMaster.com, and decided to tackle this
whole thing later. Recently I found a reasonably priced 1/4"ID 1/2"OD
aluminum tube on OnlineMetals.com. I tried it - it provides a good
tight fit for ACME screw and stepper motor shaft, little less so for
1/4" all-thread rod. I still need to test whether rod slips with the
tightened set screw - hopefully not. However, the problem with coupling
it to the 10-24 size rod remains. One of the earlier reasons that I
used 10-24 rod as opposed to 1/4" was the lower price of bearings and
pulleys on McMaster.com. However, with some searching one can easily
find 1/4"ID bearings and pulleys elsewhere for less than 3/16"ID on
McMaster. I ordered those to try and I'm thinking to switch entirely to
1/4" leadscrew/shaft size, which would eliminate the coupling problem.
However, 1/4" leadscrew requirement makes it difficult to use the
all-thread/coupling nut combination, because 1/4" coupling nut (vs
3/16") needs a lot more filing to fit in the corner of the sliding
element.
Delrin nut

Making several Delrin split nuts for
sliding elements took a while. Trying to make them faster, I rushed
somewhat which resulted in alignment problems with some of the nuts -
the leadscrew would go off about quarter of an inch or so away from the
rail for every foot. This means that some leadscrews will whip and hit
against the inner walls of the sliding elements, creating vibration,
wear, noise, accuracy problems. While it was possible to make the lead
nuts with better alignment, it would take more time and effort.
Ideally, the alignment should not be fixed so that the nut position
could be adjusted during assembly. To achieve this flexibility - given extremely limited space in the
corner of the sliding element tube, the leadnut would probably have to
be moved (with the leadscrew axis) to the center of the sliding
element. The component, carrying Delrin (or coupling) nut, would be
attached with screws to one wall of the sliding element. I made one
draft design of the centrally located leadnut. However, this is a big
change impacting many other components - leadscrew supports (rod
mounts), belt drive, motor mount etc, and it needs to be thought
through. Maybe both options should be available.
Steppers/Stepper driver
Looking for inexpensive, low current replacement for Alltronics stepper motors, I found a
$20 stepper
which seems to fit the bill - 12V, 0.4A - well under 2A limit of the
stepper driver board, with 111 oz/in holding torque (Alltronics are
rated at 60 oz/in). I need to order and test one out. Also, there is a
beefier stepper driver board apparently in works for RepRap, which I think could be used with existing 2.3A Alltronics steppers.
Minirouter

This
is the next contraption that I'm going to build from the set. I hope it
will be be stiff enough to mill wood and plastic with a dremel. Another
task for it - I need to drill a large number of tiny holes in the
cutting mat to make the vacuum table surface for the Paper Prototyper.
Finally, I'm planning to build RepRap thermoplastic extruder. This,
together with Minirouter, will make a Repstrap.